Ohio Aluminum Industries

Ohio Aluminum Industries PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages : 4

Get Book Here

Book Description
In 2001, Ohio Aluminum Industries implemented the first phase of a compressed air system improvement project at its Cleveland, Ohio, plant. By completing this phase, the plant stabilized the system's pressure and improved its performance. Furthermore, it yielded annual energy savings of 716,000 kilowatt-hours and $73,200. The total cost for the project's first phase was $83,500, making the simple payback slightly more than 1 year.

Ohio Aluminum Industries

Ohio Aluminum Industries PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages : 4

Get Book Here

Book Description
In 2001, Ohio Aluminum Industries implemented the first phase of a compressed air system improvement project at its Cleveland, Ohio, plant. By completing this phase, the plant stabilized the system's pressure and improved its performance. Furthermore, it yielded annual energy savings of 716,000 kilowatt-hours and $73,200. The total cost for the project's first phase was $83,500, making the simple payback slightly more than 1 year.

Ohio Aluminum Industries: Compressed Air System Improvement Project Saves Energy and Improves Product Quality

Ohio Aluminum Industries: Compressed Air System Improvement Project Saves Energy and Improves Product Quality PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages : 0

Get Book Here

Book Description
In 2001, Ohio Aluminum Industries implemented the first phase of a compressed air system improvement project at its Cleveland, Ohio, plant. By completing this phase, the plant stabilized the system's pressure and improved its performance. Furthermore, it yielded annual energy savings of 716,000 kilowatt-hours and $73,200. The total cost for the project's first phase was $83,500, making the simplepayback slightly more than 1 year.

Compressed Air System Improvement Project Saves Foundry Energy and Increases Production

Compressed Air System Improvement Project Saves Foundry Energy and Increases Production PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages : 6

Get Book Here

Book Description
This case study highlights International Truck and Engine Corporation's optimization project on the compressed air system that serves its foundry, Indianapolis Casting Corporation. Due to the project's implementation, the system's efficiency was greatly improved, allowing the foundry to operate with less compressor capacity, which resulted in reduced energy consumption, significant maintenance savings, and more reliable production.

Compressed Air System Improvement Project Saves Foundry Energy and Increases Production

Compressed Air System Improvement Project Saves Foundry Energy and Increases Production PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages : 0

Get Book Here

Book Description
This case study highlights International Truck and Engine Corporation's optimization project on the compressed air system that serves its foundry, Indianapolis Casting Corporation. Due to the project's implementation, the system's efficiency was greatly improved, allowing the foundry to operate with less compressor capacity, which resulted in reduced energy consumption, significant maintenancesavings, and more reliable production.

Compressed Air System Optimization Project Saves Energy and Improves Production at a Citation Forging Plant

Compressed Air System Optimization Project Saves Energy and Improves Production at a Citation Forging Plant PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages :

Get Book Here

Book Description
In the 1990s, a subsidiary of the Citation Corporation, Interstate Forging, implemented a compressed air system improvement project at its Milwaukee, Wisconsin, forging plant. This improvement enabled the plant to maintain an adequate and stable pressure level using fewer compressors, which led to improved product quality and lower production downtime. The project also yielded annual energy savings of 820,000 kWh and $45,000. With a total project cost of $67,000, the plant achieved a simple payback of just 1.5 years.

Weyerhaeuser :.

Weyerhaeuser :. PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages :

Get Book Here

Book Description


Compressed Air System Optimization Saves Energy and Improves Production at a Textile Manufacturing Mill (Peerless Division, Thomaston Mills, Inc.)

Compressed Air System Optimization Saves Energy and Improves Production at a Textile Manufacturing Mill (Peerless Division, Thomaston Mills, Inc.) PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages : 5

Get Book Here

Book Description
This case study is one in a series on industrial firms who are implementing energy efficient technologies and system improvements into their manufacturing processes. This case study documents the activities, savings, and lessons learned on the textile manufacturing mill project.

Compressed Air System Optimization Project Improves Production at a Metal Forging Plant (Modern Forge, TN, Plant).

Compressed Air System Optimization Project Improves Production at a Metal Forging Plant (Modern Forge, TN, Plant). PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages :

Get Book Here

Book Description
In 1995, Modern Forge of Tennessee implemented a compressed air system improvement project at its Piney Flats, Tennessee, forging plant. Due to the project's implementation, the plant was able to operate with fewer compressors and improve its product quality, thus allowing it to increase productivity. The project also resulted in considerable energy and maintenance savings.

Compressed Air System Upgrade Results in Substantial Energy Savings. Office of Industrial Technologies (OIT) BestPractices Project Case Study

Compressed Air System Upgrade Results in Substantial Energy Savings. Office of Industrial Technologies (OIT) BestPractices Project Case Study PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages : 0

Get Book Here

Book Description
This case study highlights a compressed air system upgrade at BWX Technologies manufacturing plant in Lynchburg, Virginia, which replaced antiquated compressors and dryers and implemented an improved control strategy, resulting in improved energy efficiency and savings in energy and maintenance costs.

Compressed Air System Optimization Improves Production and Saves Energy at a Satellite Manufacturer

Compressed Air System Optimization Improves Production and Saves Energy at a Satellite Manufacturer PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages :

Get Book Here

Book Description
In 2001, a compressed air improvement project was implemented following an audit on the compressed air system at Boeing Satellite Systems (formerly Hughes Space & Communications Company) in Los Angeles, California.