Experimental Investigation of the Performance of a Mach-2. 7 Two-Dimensional Bifurcated Duct Inlet with 30 Percent Internal Contraction

Experimental Investigation of the Performance of a Mach-2. 7 Two-Dimensional Bifurcated Duct Inlet with 30 Percent Internal Contraction PDF Author: National Aeronautics and Space Administration (NASA)
Publisher: Createspace Independent Publishing Platform
ISBN: 9781722219505
Category :
Languages : en
Pages : 46

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Book Description
An experimental study was conducted to determine the performance of a two-dimensional, mixed-compression bifurcated duct inlet system designed for a free-stream Mach number of 2.7. Thirty percent of the supersonic area contraction occurred internally. A movable ramp was used to vary the contraction ratio for off-design operation. Boundary layer bleed regions were located on the cowl, centerbody, and sidewall surfaces. There were also provisions for vortex generators on the cowl and centerbody of the subsonic diffuser. Data were obtained over the Mach number range of 2.0 to 2.8 and at angles of yaw from 0 deg. to the maximum value prior to inlet un-start. The test at Mach 2.8 was to obtain data for an over- speed condition. The Reynolds number varied from 2.5 to 2.3 million/ft for Mach numbers above 2.5. At Mach numbers of 2.5 and lower, the Reynolds number was set at 2.5 million/ft. Bleed patterns, vortex generator patterns, and ramp position were varied, and three inlet configurations were selected for more extensive study. Two of these configurations had self-starting capability. The self-starting configuration that was developed produced 89 percent total pressure recovery at the compressor face station with 6.8 percent total bleed. The compressor face distortion was about 16 percent. Vortex generators were extremely effective in re-distributing flow but were not as effective in reducing distortion. Excellent flow symmetry was achieved between the separated halves of the inlet, and twin-duct instability was not observed. The ramp tip shock was steeper than expected. This caused the cowl lip shock to be reflected from the ramp instead of being cancelled at the shoulder. However, peak recovery at the throat was still obtained with the ramp near the design position. Wasserbauer, J. F. and Meleason, E. T. and Burstadt, P. L. Glenn Research Center RTOP 537-02-23...

Experimental Investigation of the Performance of a Mach-2.7 Two-dimensional Bifurcated Duct Inlet with 30 Percent Internal Contraction

Experimental Investigation of the Performance of a Mach-2.7 Two-dimensional Bifurcated Duct Inlet with 30 Percent Internal Contraction PDF Author: Joseph F. Wasserbauer
Publisher:
ISBN:
Category :
Languages : en
Pages : 50

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Book Description
An experimental study was conducted to determine the performance of a two-dimensional, mixed-compression bifurcated duct inlet system designed for a free-stream Mach number of 2.7. Thirty percent of the supersonic area contraction occurred internally. A movable ramp was used to vary the contraction ratio for off-design operation. Boundary layer bleed regions were located on the cowl, centerbody, and sidewall surfaces. There were also provisions for vortex generators on the cowl and centerbody of the subsonic diffuser. Data were obtained over the Mach number range of 2.0 to 2.8 and at angles of yaw from 0 deg. to the maximum value prior to inlet un-start. The test at Mach 2.8 was to obtain data for an over- speed condition. The Reynolds number varied from 2.5 to 2.3 million/ft for Mach numbers above 2.5. At Mach numbers of 2.5 and lower, the Reynolds number was set at 2.5 million/ft. Bleed patterns, vortex generator patterns, and ramp position were varied, and three inlet configurations were selected for more extensive study. Two of these configurations had self-starting capability. The self-starting configuration that was developed produced 89 percent total pressure recovery at the compressor face station with 6.8 percent total bleed. The compressor face distortion was about 16 percent. Vortex generators were extremely effective in re-distributing flow but were not as effective in reducing distortion. Excellent flow symmetry was achieved between the separated halves of the inlet, and twin-duct instability was not observed. The ramp tip shock was steeper than expected. This caused the cowl lip shock to be reflected from the ramp instead of being cancelled at the shoulder. However, peak recovery at the throat was still obtained with the ramp near the design position.

Experimental Investigation of a Large-scale, Two-dimensional, Mixed-compression Inlet System

Experimental Investigation of a Large-scale, Two-dimensional, Mixed-compression Inlet System PDF Author: Norman D. Wong
Publisher:
ISBN:
Category : Jet engines
Languages : en
Pages : 68

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Book Description
A large-scale, variable-geometry inlet model with a design Mach number of 3.0 was tested at Mach numbers from 1.55 to 3.2. Variable features of the inlet for off-design operation are an adjustable-height ramp system and a translating cowl. This report presents experimental results for a diffuser and boundary-layer bleed configuration which was optimized at the design Mach number. Overall performance was high with throat-mounted vortex generators, which were effective in reducing flow distortion in the subsonic diffuser at the higher Mach numbers.

Study of Compressible Flow Through a Rectangular-to-semiannular Transition Duct

Study of Compressible Flow Through a Rectangular-to-semiannular Transition Duct PDF Author: Jeffry Foster
Publisher:
ISBN:
Category :
Languages : en
Pages : 66

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Study of Compressible Flow Through a Rectangular-to-semiannular Transition Duct

Study of Compressible Flow Through a Rectangular-to-semiannular Transition Duct PDF Author:
Publisher:
ISBN:
Category : Aerodynamics, Supersonic
Languages : en
Pages : 66

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Experimental Investigation of a Large Scale, Two-dimensional, Mixed-compression Inlet System

Experimental Investigation of a Large Scale, Two-dimensional, Mixed-compression Inlet System PDF Author: Warren E. Anderson
Publisher:
ISBN:
Category : Jet engines
Languages : en
Pages : 68

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Investigation of the Performance and Control of a Mach 3.0, Two-dimensional, External-internal-compression Inlet

Investigation of the Performance and Control of a Mach 3.0, Two-dimensional, External-internal-compression Inlet PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages : 38

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Experimental Investigation of a Large-scale, Two-dimensional, Mixed-compression Inlet System

Experimental Investigation of a Large-scale, Two-dimensional, Mixed-compression Inlet System PDF Author: Norman D. Wong
Publisher:
ISBN:
Category : Drag (Aerodynamics)
Languages : en
Pages : 52

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A large scale, variable-geometry inlet system with a design Mach number of 3.0 was tested at Mach numbers from 0.6 to 1.28. Variable features for off-design operation are an adjustable-height ramp system and a translating cowl.

Experimental Investigation of Dynamic Distortion in a Mach 2.50 Inlet with 60 Percent Internal Contraction and Its Effect on Turbojet Stall Margin

Experimental Investigation of Dynamic Distortion in a Mach 2.50 Inlet with 60 Percent Internal Contraction and Its Effect on Turbojet Stall Margin PDF Author: James E. Calogeras
Publisher:
ISBN:
Category :
Languages : en
Pages : 80

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A Full Navier-Stokes Analysis of Subsonic Diffuser of a Bifurcated 70/30 Supersonic Inlet for High Speed Civil Transport Application

A Full Navier-Stokes Analysis of Subsonic Diffuser of a Bifurcated 70/30 Supersonic Inlet for High Speed Civil Transport Application PDF Author:
Publisher:
ISBN:
Category :
Languages : en
Pages : 22

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